The westbound Zephyr got stuck at Union Station for over four hours this morning due to a motive power issue. When it arrived, AMTK 816 had been leading. Before it could depart west, AMTK 816 had to be swapped with AMTK 63. Without knowing for certain, the speculation is that there was a problem with the HEP (Head End Power) with AMTK 63, so it had to be swapped with AMTK 816, allowing AMTK 816 to become the unit providing power to the train. In any case, the train is on the move and crossing over Clear Creek on Main 2 in the OS at C&S Junction.
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